Saturday, 27 March 2010

Putting it all back together

Well I have spent the day putting the Spitfire back together after last weeks gearbox and engine out. I have fitted a new Fuse box and re wired the reverse light as it grounded out on the 10CR causing the loom to burn through. Everything sorted and the bonnet back on I have put the battery on charge to enable me to give her a run tomorrow.

Some bad news, In June/July last year someone reversed into the rear of my Spit dinting the rear bumper. I took it off today and tried to knock the dint out. No luck the Chrome has cracked so the bumper is staying off until I can get a replacement or get this one repaired and re-chromed.

I am going to wash the car tomorrow and I am off to the Lake District on Monday.

I hopefully will have the car sorted for good Friday when I hope to take her to the P&P meeting.

Fingers crossed with no gearbox leaks.

Tuesday, 23 March 2010

Finally.



Well after finishing my Exam and having a little more time on my hands I managed to do a little on the Megasquirt assembly. Well to say a little would be an understatement.

I finished the board a couple of days after my exam which was on the 9th March, and after plugging it into the stimulator, I heard a little click and the computer refused to communicate with the Daughter-board (main chip). After removing the Daughter-board I checked the voltages on the mount finding 2.5volts where 5volts should have been!

Well after panicking and fearing I had burnt the whole lot out, I followed the trouble shooting instructions on the Megasquirt main site, I checked all the build steps one by one and found nothing. So I went onto the Megasquirt Forum, where it is clear I am a novice at this, The fella I bought the kit from asked if Diode D19 (Capacitor 0.1µF 50V 10% CER RADIAL - X7R) was getting hot! Sure enough it was.

His suggestion was check all the board for bridged solder joints and replace Diode D19.

On checking the board out with a magnifying glass I found I had bridged the 12volt and the 5volt lines on Q1 which a (field effect transistors, used to drive the injectors) It was only a very very small bridge but this had burnt out D19 which regulates and protects the 5v circuit.

Now the tricky bit, get hold of a (Capacitor 0.1µF 50V 10% CER RADIAL - X7R) Maplins did not stock this item; other sites sold them but only in the 1000's. But as always I turned to EBay and found them in a shop in Japan. £2.99 for 50. They were only available in 50's so at three quid I placed the order.

Well I am pleased to say the Capacitors arrived today and I fitted the 1 needed and hey presto a fully working Megasquirt.

I have tested it on the Laptop with the Stimulator and all seems fine, I have loaded a basic Map and injection table to test the board and all seems superb.


What a relief!


Rob

Saturday, 6 March 2010

Megasquirt/ Mega Stimulator

Ok After frying my brains with revision for what seems like forever I have taken a few hours break to clear my head. The Exam is on Tuesday and I can then concentrate on getting the Megasquirt built.

However I have managed to build the Mega Stim (used to check the Megasquirt as I build it) this was built the other night with a beer. (after 9 hours revision I needed a break) I was genuinely surprised with the quality of my soldering (much better than my previous work on the megajolt).
One thing I have noticed from the outset is the superb quality of the Megasquirt kit. It has clear labels on all parts and the quality of the board itself and the instructions are outstanding.

I have started to build the board and have completed steps 1 to 22, I have stopped whilst I figure out what IAC (idle air control) valve I will use and where to place this in my set up.


The IAC helps smooth out the start up sequence.

Pictures attached and as usual any questions or comments appreciated.

Rob

Wednesday, 24 February 2010

Injection.



Well after a lot of thought and reading up on the Hows and What if's I have decided to inject the Spit.
This will not be an overnight operation as I am planning to fabricate my own inlet and Plenum chamber as well as building the Megasquirt engine management unit myself.



The kit came today and it looks a superb quality piece of kit. More on this soon.


I have been busy with revision for an upcoming exam, however I am not holding my breath as I have been ultra busy at work and the last thing I have been wanting to do after a 18 hour day is revise. Well with the next few weeks off I plan to cram and cram. Fingers Crossed eh.

I have done a little on the car, the bonnet is off again waiting for the engine to come out for a bit of work on the gearbox seals again. I have also bought a new engine crane as the previous lift belonged to Bob King and I was going over and above the friendship barrier as I have had his lift more than he has over the last 12 months.



Well any Question please drop me a mail.

Rob

Tuesday, 26 January 2010

P&P Not the Xmas meal.

On the first Friday of 2010 the usual suspects + some very welcome guests visited the local meet for what is known as 'Not the xmas meal' Where good food and lots of drink were consumed. Gluggg.


Steve Thompson won the P&P trophy this year as he had attended every meet in his Triumph as well as earned a few well earned bonus points.

I was refered to as Bobybroken Spit ,LOL.

I hope to have the car back on the road fully fit for the La Carrera Cannonball or its replacement event which I am really looking forward to after last years FlusterMuc of an event. BRING IT ON.

Sunday, 15 November 2009

RBRR 2010.


Ok guys, car 59 its official.
I am now working hard at working out my niggles.
and there are lots.
I took the car out last week to Oulton Park and the carbs need setting up, the engine cut out on a few occassions which is down to the electrics! A fiddle with the ignition restored running.
Well a new fuse box will need to be fitted, new seals on the gearbox, a full set up on the carb will be needed. I have a load of other jobs like checking UJ's and changing the silicone to mineral!
I will as always try to keep this blog more updated than the other half of Team Insulated Shorts,
Steve Thomspon.
Keep an eye on the blog for regular updates.
Rob

Saturday, 10 October 2009

BRUM BRUM






With a few hours work and assistance as always from Tiggrr (Steve Thompson) the Broken beasie is now running again.




I had the head apart for a clean and re seat the valves and building the engine back up again before a nice test drive. The carbs need a little balancing and the battery needs charging other than that all seems well.




Thanks again to Steve, owe you a few pints mate.